Hey,
does anyone have an idea what is wrong with my mobula6? Here is some DVR showing the twiches.
https://drive.google.com/file/d/1fW5mMIbSeJQvaS42cBqddw-g-ska40OM/view?usp=drive_link
(Be careful with your volume. Loud analog sounds)
I already replaced all 4 motors. It did not help...
Thanks in advance!
Hey,
thank you all for your help.
I managed to fix it by going to the Happymodel manual and resetting my config back to the values shown there. (How did I not think of this myself???)
https://www.happymodel.cn/wp-content/uploads/2024/01/Mobula6-2024-1S-65mm-micro-fpv-whoop-manual.pdf
(Except or the First gyro angle. the manual shows 0°, but it is 90° on my whoop for some reason...)
Tell us more about what the problem is.
Could be the wrong number of poles in BF.
But also a wrong angle in the ESC setting.
But without a more detailed description of the problem it is a search in the dark
Christian
I'd a look at your video. ESC aside , it could be many things causing that ie mechanical or your config.
Are your props in good nick ?
Is your build reasonably clean ?
Have you selected filters for clean build or noisy build and selected the correct packet rate (match to controller) for RC link if using ELRS. ?
Dterm too high ? Not tuned right ?
Send screenshot of your pids and filters.
Hey,
thank you all for your help.
I managed to fix it by going to the Happymodel manual and resetting my config back to the values shown there. (How did I not think of this myself???)
https://www.happymodel.cn/wp-content/uploads/2024/01/Mobula6-2024-1S-65mm-micro-fpv-whoop-manual.pdf
(Except or the First gyro angle. the manual shows 0°, but it is 90° on my whoop for some reason...)
Ist ungewöhnlich wenn die Startwerte so hoch sind. Mit der Standart Setup sollte es laufen.
Hey, to start with here are my ESC Settings.